Hello all,
I've finished my first bit of purposeful ally welding, although I think I'd give myself a relatively low mark on the absolute quality of the welds.
Successes
- Well, it's together!
- Some welds came out well
-Technique is improving
Not-so successes
- Caused material drop out in places, particularly the top piece which I welded with the hole stand upside down (legs onto top piece)
- Bach sides of the angle section joins look not nice!
- Some welds displayed a 'micro-bubbly' surface - don't know why
Learning points
- Get the weld pool shiny before doing anything with it
- The twisted filler wire tip to make an equivalent larger filler rod worked well
- Preheating (see pic) helped a bit
- Designing the piece so that I don't have a thinner (3mm) piece welding to a thicker (5mm base) in a perpendicular fillet.
- The better the fit up the better the weld
- Don't bevel every edge to make a vee channel to weld into.
- Ally sucks amps - if I were doing a lot of this I'd coonsider a machine with more amps! (although I haven't gone above 140 A yet since 'I got scared' - machine is a 160A)
- Higher frequency concentrates the weld pool
- Tight electode gap improves cleaning (should have played with cleaning/EP/EN balance instead of leaving it at 50% though)
- Give the arc time to get rid of the black floaty bits in the weld.
Any tips, particularly on the micro blisters in the wled surface, much appreicated!
I've finished my first bit of purposeful ally welding, although I think I'd give myself a relatively low mark on the absolute quality of the welds.
Successes
- Well, it's together!
- Some welds came out well
-Technique is improving
Not-so successes
- Caused material drop out in places, particularly the top piece which I welded with the hole stand upside down (legs onto top piece)
- Bach sides of the angle section joins look not nice!
- Some welds displayed a 'micro-bubbly' surface - don't know why
Learning points
- Get the weld pool shiny before doing anything with it
- The twisted filler wire tip to make an equivalent larger filler rod worked well
- Preheating (see pic) helped a bit
- Designing the piece so that I don't have a thinner (3mm) piece welding to a thicker (5mm base) in a perpendicular fillet.
- The better the fit up the better the weld
- Don't bevel every edge to make a vee channel to weld into.
- Ally sucks amps - if I were doing a lot of this I'd coonsider a machine with more amps! (although I haven't gone above 140 A yet since 'I got scared' - machine is a 160A)
- Higher frequency concentrates the weld pool
- Tight electode gap improves cleaning (should have played with cleaning/EP/EN balance instead of leaving it at 50% though)
- Give the arc time to get rid of the black floaty bits in the weld.
Any tips, particularly on the micro blisters in the wled surface, much appreicated!